...
首页> 外文期刊>E3S Web of Conferences >Improving the efficiency of well workover solutions for the elimination of behind-the-casing flows
【24h】

Improving the efficiency of well workover solutions for the elimination of behind-the-casing flows

机译:提高井下工作型解决方案的效率,以消除壳体流动

获取原文
           

摘要

The article deals with the increase of profitability of water shutoff treatment (WST), which is used to eliminate behind-the-casing flows (cross-flow) in production and injection wells. It is presented that modern technologies of water shut-off works have low efficiency (success rate), especially in liquidation of non-perforating interval. Inefficient (wasteful) injection is currently one of the main problems in the development of oil and gas fields, as it significantly reduces the oil recovery factor in addition to the huge costs for oil companies for injection (operating costs). The article presents the results of hydrodynamic research and proposes methods for determining the presence of behind-the-casing flows (BCF) and methods for detecting wasteful injection without geophysical well-logging (a non-standard approach). The article also presents equipment for the elimination of the behind-the-casing flow and technology of its implementation.
机译:本文涉及水截止治疗盈利能力(WST)的增加,用于消除生产和注射井的外壳流动(交叉流量)。 据介绍,现代水关闭工程技术效率低(成功率),尤其是在无孔间间隔的清算中。 效率低(浪费)注射目前是石油和天然气开发中的主要问题之一,因为它除了用于注射的石油公司的巨额成本(运营成本)之外,还会显着降低石油回收率。 本文介绍了流体动力学研究的结果,提出了确定壳体后面流动(BCF)的存在的方法和用于检测浪费注射的方法,而无需地球物理良好测井(非标准方法)。 本文还提供了消除套管背后流量和其实施技术的设备。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号