首页> 外文期刊>Seismological research letters >Seismic Moment Tensor Inversion of an Induced Microseismic Event, Offshore Norway: An Insight into the Possible Cause of Wellbore Liner Failure during a Drilling Operation
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Seismic Moment Tensor Inversion of an Induced Microseismic Event, Offshore Norway: An Insight into the Possible Cause of Wellbore Liner Failure during a Drilling Operation

机译:Seismic Moment Tensor Inversion of an Induced Microseismic Event, Offshore Norway: An Insight into the Possible Cause of Wellbore Liner Failure during a Drilling Operation

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摘要

A microseismic event with M-w similar to 0.8 was recorded at the Grane oilfield, offshore Norway, in June 2015. This event is believed to be associated with a failure of the wellbore liner in well 25/11-G-8 A. The failure mechanism has been difficult to explain from drilling parameters and operational logs alone. In this study, we analyzed the detected microseismic event to shed light on the possible cause of this event. We inverted for the seismic moment tensor, analyzed the S/P amplitude ratio and radiation pattern of seismic waves, and then correlated the microseismic data with the drilling reports. The inverted seismic moment indicates a shear-tensile (dislocation) event with a strong positive isotropic component (67% of total energy) accompanied by a positive compensated linear vector dipole (CLVD) and a reverse double-couple (DC) component. Drilling logs show a strong correlation between high pump pressure and the occurrence of several microseismic events during the drilling of the well. The strongest microseismic event ( M-w similar to 0.8) occurred during peak pump pressure of 277 bar. The application of high pump pressure was associated with an attempt to release the liner hanger running tool (RT) in the well, which had been obstructed. Improper setting of the liner hanger could have caused the forces from the RT release to be transferred to the liner and might have resulted in ripping and parting of the pipe. The possible direct impact of the ripped liner with the formation or the likely sudden hydraulic pressure exposure to the formation caused by the liner ripping may explain the estimated isotropic component in the moment tensor inversion in the well. This impact can promote slip along the pre-existing fractures (the DC component). The presence of gas in the formation or the funneled fluid to the formation caused by the liner ripping may explain the CLVD component.

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