首页> 中文期刊> 《油气田地面工程》 >下游间歇用气的天然气连续脱烃生产方案

下游间歇用气的天然气连续脱烃生产方案

         

摘要

南山终端进入下游间歇用气的小流量生产阶段后,出现了天然气烃露点控制不稳定、环境对低温脱烃系统影响加剧、恢复供气耗时长、火炬放空量大等问题。针对上述问题,对流程进行了优化改造:并联安装一个小流量副J-T阀,全面增强低温脱烃系统的保冷效果;调整生产操作方式,执行小流量供气模式。通过上述优化改造,可保持天然气连续脱烃生产,每年天然气减少排放量达到304×104 m3,实现节能增效。%Nanshan terminal is now in the low flow gas production stage with downstream user intermittent using gas, for such problems as natural gas dew point controlled unstable, environmental increased effects on low temperature de-hydrocarbon system, longer period of restored gas supply time, large amount of flare venting, etc., so an optimization scheme was taken to reengineer the flow processing. A by-pass secondary J-T valve was parallel in-stalled for low flow controlling to enhance the insulation effects of low temperature de-hy-drocarbon system; the operation procedures was adjusted to low gas supply flow mode. The result shows that natural gas de-hydrocarbon production could work continuously, the re-duction amount of flare gas emissions is 304 × 104 m3 yearly, the energy consumption is re-duced and efficiency is increased accordingly.

著录项

相似文献

  • 中文文献
  • 外文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号