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首页> 外文期刊>Advances in civil engineering >Study on Permeability Improvement Technology by Injecting Air into the Gas Drainage Borehole in Low-Permeability Coal Seam
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Study on Permeability Improvement Technology by Injecting Air into the Gas Drainage Borehole in Low-Permeability Coal Seam

机译:向低渗煤层瓦斯抽放钻孔注气改善透气性的技术研究

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Gas extraction cycle is too long in low-permeability coal seam. In order to solve the problem, the basic principle about gas drainage drilling for gas injection technology is studied to increase permeability. And the mathematical model is established. Gas is injected into the low-permeability coal seam by numerical simulation. The results indicate that the best condition is a negative pressure drainage at 26 kPa and a gas injection pressure at 0.6 MPa in the vertical direction and in the horizontal direction of the injection hole. In Shanxi Daping Coal Mine 3113 working face, the field test is implemented. As a result, the test is successful. During the 14 d gas injection constantly, gas content of coal seam is reduced from 12.33 m3/t to 7.12 m3/t, greatly reducing the risk of coal and gas outburst elimination time required.
机译:低渗透煤层瓦斯抽采周期过长。为了解决该问题,研究了注气技术抽放气的基本原理,以提高渗透率。建立了数学模型。通过数值模拟将气体注入低渗煤层。结果表明,最佳条件是在注入孔的垂直方向和水平方向上的负压排放为26 kPa,气体注入压力为0.6 MPa。在山西大坪煤矿3113工作面进行了现场测试。结果,测试成功。在持续注气14d的过程中,煤层的瓦斯含量从12.33 m3 / t降低到7.12 m3 / t,大大降低了消除煤与瓦斯突出所需时间的风险。

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