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首页> 外文期刊>Journal of Quality and Reliability Engineering >Productivity Improvement of a Special Purpose Machine Using DMAIC Principles: A Case Study
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Productivity Improvement of a Special Purpose Machine Using DMAIC Principles: A Case Study

机译:使用DMAIC原理提高专用机的生产率:一个案例研究

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摘要

Six Sigma is one of the popular methodologies used by the companies to improve the quality and productivity. It uses a detailed analysis of the process to determine the causes of the problem and proposes a successful improvement. Various approaches are adopted while following Six Sigma methodologies and one of them is DMAIC. The successful implementation of DMAIC and FTA is discussed in this paper. In this study, the major problem was of continuous rework up to 16%, which was leading to wastage of man hours and labor cost. Initially, fault tree analysis (FTA) was used to detect the key process input variables (KPIVs) affecting the output. Multivariable regression analysis was performed to know the possible relationship between the KPIVs and the output. The DMAIC methodology was successfully implemented to reduce the rework from 16% bores per month to 2.20% bores per month. The other problem of nonuniform step bores was also reduced significantly.
机译:六西格码是公司用来提高质量和生产率的流行方法之一。它使用对过程的详细分析来确定问题的原因并提出成功的改进方案。在遵循六西格码方法的同时采用了各种方法,其中一种是DMAIC。本文讨论了DMAIC和FTA的成功实施。在这项研究中,主要问题是连续返工率高达16%,这导致工时和人工成本的浪费。最初,故障树分析(FTA)用于检测影响输出的关键过程输入变量(KPIV)。进行多变量回归分析以了解KPIV和输出之间的可能关系。 DMAIC方法已成功实施,可将返工率从每月16%减少到每月2.20%。不均匀阶梯孔的另一个问题也大大减少了。

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